2007 deleted Maxxforce DT. Just rebuilt with new pistons, rods, mains, head, pucks, cam sensor, MIT, MAP, IPR, ICP, and 1 new injector. Start truck and runs perfect when cold. Heats up to about 170-180 degrees and begins to misfire and white smoke will come out so bad the fire department gets called (literally). Had another mechanic come over and hook computer up (not maxxservice) and the only code that comes up is not enough exhaust back pressure. Checked valves several times and they are to spec. Took turbo off to see if any change, nothing. Took exhaust manifold off to see what cylinder was smoking, all 6. The exhaust side of head where the new injector is located is soaked with fuel. Switched injector 1 and 2 to see if the new injector made the number 2 exhaust hole on head wet and it did. On one of these threads it stated injectors have to be reprogrammed when replaced. The delete was done before motor was rebuilt and truck ran fine until the #2 cylinder failed. Local International dealer will not answer any questions since it’s been deleted. Any ideas on what else to check?
2007 Deleted Maxxforce DT excessive smoke and misfire
Discussion in 'International Forum' started by dredge54, Apr 27, 2020.